While it was a short week and I wasn’t able to spend as much time on my project as I would have liked, I still accomplished some of the more impressive steps to date and am very pleased with where I am.
Having been out of town on Saturday, Sunday and Monday of last week, I got back to work on Tuesday evening by first removing all my clamps from where I left them last Friday and then cutting out the F-holes in the soundboard.
As I started to cut the F-holes I was a little nervous about this step since the soundboard is so thin (as little as .01”) and I was planning to use a powered scroll saw to do the work. My fear, naturally, was that the scroll saw would cause cracks or some kind of chipping. My other option was to try to cut these manually using a hand-held scroll saw with one hand while trying to steady the soundboard with the other. While the manual method would likely help prevent chipping and cracking, I opted for better material handling control and went with the powered method. I figured the gauze I glued in earlier was my insurance against damage. As Mr. Siminoff suggested, I made sure to cut slowly.
I started by drilling four holes, one in the center of each scroll “balls” (best description I can think of on short notice) using a small 1/6” bit as a pilot followed with a larger 1/4” bit which is big enough to allow the scroll saw blade to be inserted. Then with these four holes drilled, I moved over to the scroll saw and began cutting.
As I did this next step, I learned something - cut out the ball first and then cut the long stretches. Here is why; as I made the cut around the ball, the “stretch” cut (my term) completed earlier, I found that the wood was vibrating badly and realized that the inside point where the stretch cut meets the ball was having to handle all that vibration with no support. Had I cut the ball first and then the stretch, starting the stretch cut at the point, the stress from the vibration would have been shared by a lot more wood rather than just the point. I hope that makes sense.
In any case, the points on this first F-hole made it through my abuse and I went successfully on with the second one much happier with my new-found insight. Here are some photos of the finished results after some sanding.
That pretty much did it for Tuesday night.
Wednesday I started with the tone bars. Back when I started this project, I made it a point to save pretty much all my scrap wood so, when it came time to make these, I was able to cut them out of the scrap pieces I saved from the blanks used to make the soundboard itself. Once I had cut out my tone bar blanks as per the dimensions in the book, I needed a way to transfer the shape of the inside curve of the soundboard to the bars so I could cut them to fit. To do this I went about as simple as it gets. I took a small piece of scrap side wood and taped on some lead from my mechanical pencil. Holding this in my right hand while holding the tone bar blanks in position with my left, I gently traced the curvature onto the blanks.
Then it was time to glue them in place. For this, I used three clamps one each tone bar with leather cauls on the back side of each clamp and a board on the from to help distribute the pleasure more evenly. As with most gluing procedures, I finished of the night with this step and left them to dry for 24 hours.
Thursday I removed the clamps and did an initial crowing and cleaned the edges of the joints between the bars and the soundboard.
For this, I used my 40 cello clamps, the side mold for reference, and hide glue. After preparing the clamps and getting the hide glue to temperature, I spread the glue and worked as fast as I could to clamp the soundboard in place. Here’s how it looked with all the clamps in place.
Saturday was completely a wash as far as mandolin building goes since my wife and I decided to go to an auction that ended up lasting all day. We got some good stuff, but boy, what a day. Once we got home and got unloaded, it was about 9:00 pm, so about all I had time for was to unclamp and inspect my glue joints. It appears that contrary to my worries, my clamping speed was sufficient and the joints are tight. Here is how it came out.
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